I never updated this thread lol. Last season on the day of the NADM event... (I must not have much luck at NADM races since the truck broke for the last two years on this day lol) The truck started backfiring in high rpm and became super smoky and sluggish. Like wouldn't even make more than 20 psi. I messed around with it for 2 days changing sensors, ecm's, tunes. Finally called it and pulled my injectors to have them tested as a last resort. Test results came back with scaring on my plungers and super high return rates. Decided it was not worth the risk to run them in the motor, and I did not have money for new ones.
Ended up switching jobs in January to a full time job, going to school in the mornings. Absolutely love that decision and am happy with where I am right now.
I was able to buy some used injectors which are going in soon. I also ordered 2 FASS 220 pumps, billet hold downs, manifolds and up pipes, and an s483 single. Ended up changing my mind today and I am going to try the new s476sxe charger instead. I also have a V2 on the way and am going to attempt to tune it myself lol.
I am also in the process of stripping the frame and Repainting it, and probably have well over 20 hours put into it already.
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