Talked to Trent last night, it went 10.11 @ 124 he shut it down due to an issue it was on a lower tune on the DSP though
Well I received a package from ATS today , I talked to them at the beginning of the week and they sent me a new dual CP3 controller free of charge , some of you may have read about the problems i ran into down in Vegas last weekend with the truck not holding rail pressure . I got the new box installed today , so this evening me and my brother decided to take the truck out for a little spin to see if the fueling problem is fixed and lift our spirits a bit and damn ..................................................................................................................................................... all I have to say is its going to be interesting the next trip to the track , this mother @#$%^$ is fast as long as weather holds we are taking it out again Friday night @ the Midnight drags @ RMR .
I'm having terrible problems holding rail and my rail pressure goes up and down like a yo yo. I thought about changing the dual cp3 controller but everyone has assured me either they work or they don't. So I'm wondering how you new your controller was gone. I put a wot switch in mine and I can hold rail easy but it still goes up and down like a yo yo. Has me thinking. Best of luck working the little bugs out of your trcuk can't wait to see it run at it's potential.
Have you changed the rail pressure adjustment tables?
Talked to Trent last night, it went 10.11 @ 124 he shut it down due to an issue it was on a lower tune on the DSP though
Ya they weren't too happy but after finding out it was just water and seeing all the other stuff I have done to the truck to try and prevent spills they were ok.I know track officials were mad at him for making a swimming pool out of coolant ....
Sounds like it's spooling pretty well off the line and getting to the 330' quicker than the twins were last year. You spraying it to get the turbos to zip up? Or did you not have to? Congrats on the progress! :thumb:
clean run looked good hope nothing serious is broke
nice trent!!! truck is gunna be a freakin runner when you get her dialed in.
Nice :thumb:
Hope it was just a loose Hose Clamp ?? and no damage !!
It sounds completely different than the big twin set up. I am pretty confident that I like the way it sounds. It will get dialed in ... stand back when it does.:thumb: It looks like the radiator hose let loose at about 1000' mark or so, wonder what it would have been if it all kept together.
Sounds like it's spooling pretty well off the line and getting to the 330' quicker than the twins were last year. You spraying it to get the turbos to zip up? Or did you not have to? Congrats on the progress! :thumb:
that pass was fuel only