have you done a compression test yet? we are dying to hear what/how it is:happy2:
Tell me where to get a hold of this George guy. I'm interested.so far they are sweet ! , i ran a 1850 pulse tune today and it flat a** moved , this thing is going to be faaast ! :coolspot:
Tell me where to get a hold of this George guy. I'm interested.
Trent, your truck rocks! I hope it skedaddles like you expect it to!
Well boys and girls, the good news is that this thing flat a** flys on very little fuel , and EGT's seem to be down 100 deg also but have to see how fast the tune runs before i can say for shure if that 100 deg drop is acurate , right now i am not even hitting 1200 deg ( 1150-1175) .
The bad news is i have pressure in the cooling system so i think one or both of the cups didnt seal , for all i know it could be the head gasket, dont know for shure , have to pull the glow plugs and see if any coolant is getting in the cylinders . I am going to run it regaurdless this weekend , I rigged up a coolant catch bottle I will just have to fix it later
Well , my thoughts were correct on that it was making alot of power on very little pulse width , at the track last night ................. i wasnt able to run all night because of the coolant issue , I covered the track( coolant) so had to call it quits but put down 3 runs on my 1950 pulse tune and ET wasnt good ( 11.9) because i could spool on the line ( bad MAP sensor come to find out ) but my trap speed was 114.7 on that tune with nothing stipped full interior and even tailgate on , I wonder what it will do today on the dyno with 2750
Told you to put a bigger catch can on
That seems good for a 1950 WOW:happy2:
SO you couldnt spool because of the map sensor? That was a typo right?
I hope it went well on the dyno tonight,,,,Awaiting the results :coolspot:
yes that was a typo , the computer isnt seeing any boost , when i log it the #'s dont change, it was stuck at 4.5 Psi , I couldnt get the computer to cammand any more than 60 mm3 no matter what i changed in the tune untill i was about 20 feet out of the whole i had all 4 slicks bolted up and was getting 1.8 60 ft's , same tune as far as limmiter tables i have always ran . See dyno forum for results :coolspot:
I have never felt good about doing studs without replacing gaskets.
Hopefully it is just a cup
it is , it does not have any symptoms of a HG .
Hmm..... sounds familiar.
They have the same symptoms