Alright so I tore my trans down today and everything looked great. I took out the Transgo converter flow valve and put in my modified stock one also put the mike L PR spring in in place of the shimmed stock spring.
Got the trans back together and just went out for a test drive. Everything is running just fine and dandy! Honestly I cant tell a difference from before. Not that I was really expecting too considering all I did was raise main line pressure about 45 psi and eliminated knock down on lock up.
One thing I noticed and I'm assumingg Iis how it's supposed to be is that the new mike l pressure spring is actually shorter than the stock spring. Just from eyeing it up the new spring appears to have slightly larger diameter material. Not sure I could tell a difference in spring tension when compressing both with my fingers. The new spring was about .125" shorter than the stock spring. No doubt it was a stiff little guy...
Anyways, I'm going to get a pressure gauge and hook it up so I can see exactly what the pressures are doing and too see if i actually eliminated knock down.
Wish I would have taken more pics but i was oily all day. I got a few i will post but nothing special.
Heading out for another drive right now.