Poor fuel economy after replacing the return fuel line and 4 injectors. First time in the shop for a wrench to the motor at 149,000. The shop that did the work for me also put a valve cover gasket on and pinched it ( leak) according to the dealership ( today). Going to have the gasket replaced monday but my question is still about the change in mileage. I have owned this 02 Durmax 13 yrs since it had 2000 miles on it and I have consistently had 17 mpg empty but since the fuel rail issue I am getting 12 - 14 mpg. Truck runs great, what am I missing? Could it still be an injector problem still? The work was done at 149,00 miles and I am now at 153,000. I do very little of my own wrenching so I like to be well informed when facing a mechanic or worse yet a service writer.
One other concern ( I am not satisfied with the dealership explanation) when in 4 wh dr and I go from drive into park it makes a ratcheting sound going past R. Any suggestions?
Sent from my iPad using Tapatalk. All stock 02 lb7 EC LB XLT 4x4 dually auto Alli 5 spd
One other concern ( I am not satisfied with the dealership explanation) when in 4 wh dr and I go from drive into park it makes a ratcheting sound going past R. Any suggestions?
Sent from my iPad using Tapatalk. All stock 02 lb7 EC LB XLT 4x4 dually auto Alli 5 spd