guess i can update this a bit.
first off, i eventually found the whole issue as to why the aem would not log. as time progressed, the tracker ran shittier, it wouldnt shift right when letting it shit via auto, and hesitated like mad... Come to find out, the non-resistor racing plugs i put in there were radically screwing up the whole electical system with radio interference. DOH! I found some resistor racing plugs from summit (fricken 11 bucks each!) and put those in, thing ran perfect. put the aem in and it logged perfectly. go figure.
in the midst of all that, i bought a megasquirt MS3x so i could run the engine standalone, keep sequential fueling and spark, and have full tuning of the engine. i did the "do it yourself" version which meant soldering all the componets onto the board. took me a couple days after work but i had a blast doing it
i think this was it pretty much done. mind you, this board was completely blank when i started.
i had the wiring harness, built both the MS3 and the add on for sequential injection/spark, gm ait and coolant temp sensors, and some other things to wire this sucker in. Then disaster struck....
about a month after i finished the computer, i go to find it and get ready to install it. i cannot find the box anywhere. i start tearing apart the whole house, garage, my work, every damn place i can think of. i searched for a week straight and never found it... either someone walked off with it when we had my boys birthday party or someone thought the box was trash when cleaning up and threw it away.... no damn idea how that would happen as the box was no where near the gifts or anything else that would warrant "hey, this looks like trash, lets throw it out". so yeah... 750 bucks is either gone or trashed..... Ive not given up hope totally but im pretty sure its gone.
so rolling on, i then find the whole spark plug issue soon after and keep driving/tuning it. got it pretty well dailed in and running good. shes on 9-10psi at this point. All the while, oil pressure has not been the greatest (foreshadowing) since i did the turbo. Fast foward to August 2022
Turbo has made it about 10-12k miles, little over a year on the kit and i decide to drive the tracker up to flag to start scouting for my elk hunt. drives there and back flawlessly. roads were absolutely screwed too with all the rain Flag got. 2 days later, im headed to downtown phx and back up for some parts for work. im tuning part throttle/in boost leaning it out as i learned more info about what proper AFR's should be there and i was way rich. in doing this, its 105* out, im constantly rolling hard into boost, getting back out of it and doing it at freeways speeds/high loads. i get back close to the shop and get on it WOT to pass a guy and get my exit. Tracker feels gutless... hmmm. pull into a place to get food and as soon as i roll the window down i hear a slight engine knock. shit... get food and get back to work. rev it up sitting there at over 2k this thing is knocking like a hammer on a tin roof. RIP that poor motor. 256k and it finally had enough. part of it was my fault in not beefing up the oiling system for the turbo or adding a cooler but oh well, i wanted to push it.
Friend of mine had a donor vehicle with 160k on it. picked it up for 500 bucks and ever heard it run. i decided i would tear this engine down, completely reseal/regasket the whole thing including the HG and valve stem seals to make it as sealed up as my old engine (i hate leaks!). while i was in there, i also decided to open up the ring gaps for boost as well IF the cylinder were not that worn already. But all this had to wait till after my elk hunt.
out with the donor engine
on the stand ready for a re-seal/re-gasket
torn down to pretty much a bare block. just crank left in it. clearances looked great and rings were opened up from .011 to .016. No new rings, we are going sloppy mechanic style on this sucker. did get a new oil pump though.
pistons needed help though. rings werent "stuck" but the old fuel had them moving slow. also, all the gas ports were plugged up. little elbow grease later, ready to go back in.
button up that engine to pretty close to a long block. i needed to swap over parts from the old engine as i did mods to things or had new parts installed. i wanted to use my re-ground cams and attempted to put them in without removing the front cover of the new engine but found that wouldnt work and the cam journals of the re-grinds were not happy from low oil pressure so i decided against using them. this little issue is again, foreshadowing lol.
Pulled the tracker in to start tear down.
shes out! robbed everything i needed and was ready for the new engine install
going back in
and this is where frustrations mount. Besides the fact that you need little hands to do anything on this damn rig, when i first started it, this bitch was knocking but it was all top end knock. made no sense to me. it wasnt lifter tick or anything, it was far louder. i had enough at this point, threw my tools down and walked inside. spent the rest of the weekend with the kiddos and wife. The next weekend, i pushed myself back out into the garage and started diag. pulled the intake and valve covers to see if something was broke. nothing i could see but the cams on the driverside head were damn near locking up. If you look close, you can see the DS head looks new. Well, it kinda is. i bought it rebuilt off ebay in 2017 to go on a junk engine i had from a different GV to build into a high compression 2.7 v6. that never happened and i scrapped the engine but kept the head. decided to use it on this engine since the other head looked like it was replaced at some point and figured id save time cleaning carbon out, putting valve seals in, cleaning valves, all that junk. NOT... what i figured had happen is the ebay rebuilder didnt give a crap if the head was too warped before machining it. ill bet this head has good amount of warp to it and thats why my cams bind up. if i back the caps off just a touch, they spin perfect. i have no idea if this is the knock issue but either way, this head has to come off...
i start tear down and getting everything apart... again. ordered up another mls gasket, headbolts and other gaskets. as soon as i get the head off, i realize where the knock is coming from
those aint factory
apparently, when i tried installing the other cams, then gave up, i must have clocked the intake cam 1 tooth off and didnt realize it. fuuuuuuuuuuuuuu. i mean, atleast it was on this head lol. i threw a borescope down the other side and no valve to piston kissing going on
So what do i do? no damn way im changing pistons out but i dont want the sharp edge in there and cause detonation. So dremel comes out and i file it away. I took the old head the new engine had and "rebuilt" it (new valve seals, decarboned combustion chamber, cleaned valves, cleaned carbon out of the intake track). Then yesterday all my parts arrived so i was on a mission to get it back running. the moment i found the knock issue, it was like all my anxiety vanished and i knew how to fix it. put the whole thing back together last night from this
to this
and it purrs right along. no knocking, no chain rattle, no nothing. yyyyyyyyaaaaaaaaasssssssssssss!!!!!!!!! ill finish it up tonight and hopefully drive it to work tomorrow.
now i can finally get back to working on my shop and getting it up and going!!