"Reduced engine power" code P2138!!!! Update
Ok this is happening out of no where. I have a 2006 lbz fully built socal motor built big dipper trans everythind deleted tuned by moonshine tunes ( tony) and a ton more. Anyways truck has run perfect for a long time with zero issues. I went to camp for a week we had a bad storm on the lake started the truck up the next day drove it for about 30 mins that the " reduced engine power" display came on. This truck has never ever displayed this. There is no CEL just this display on tue DIC. Went home unhooked the negative waited about 10 mins attached restarted truck and gone. Never came back on for about 2 days of driving. Now 1 week later im driving the truck for about 2 hours and out of no where engine power decreased comes on again. Then shut the truck off to eat dinner for about 1hr and it went away. Then a few minutes driving down the road it comes back on. Every gauge is perfect. Only thing that the few times its done this ill have decreased theottle response. Im stumped on this one. Also changed the water seperator/ fuel filter air dogs about 1000 miles ago. This came out of no where and wondering if anyone has had similar issues.
Ok this is happening out of no where. I have a 2006 lbz fully built socal motor built big dipper trans everythind deleted tuned by moonshine tunes ( tony) and a ton more. Anyways truck has run perfect for a long time with zero issues. I went to camp for a week we had a bad storm on the lake started the truck up the next day drove it for about 30 mins that the " reduced engine power" display came on. This truck has never ever displayed this. There is no CEL just this display on tue DIC. Went home unhooked the negative waited about 10 mins attached restarted truck and gone. Never came back on for about 2 days of driving. Now 1 week later im driving the truck for about 2 hours and out of no where engine power decreased comes on again. Then shut the truck off to eat dinner for about 1hr and it went away. Then a few minutes driving down the road it comes back on. Every gauge is perfect. Only thing that the few times its done this ill have decreased theottle response. Im stumped on this one. Also changed the water seperator/ fuel filter air dogs about 1000 miles ago. This came out of no where and wondering if anyone has had similar issues.
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