Try injector hold downs. Mine made the same noise.
Man I hope you find something. That's EXACTLY what mine sounds like.
Not trying to steal your thread but it seems likes we're having the same problem. Here's a video of mine that might help people diagnose what's going on
http://www.youtube.com/watch?v=p2T_vZAe32w&feature=youtu.be
From that video it sounds like excessive valve lash to me. I would pull the valve cover and recheck it.
From that video it sounds like excessive valve lash to me. I would pull the valve cover and recheck it.
X2
the valves should be reset anytime you pull the heads off
Valves were done to .011. Triple checked them but I guess it could be off.
I just swapped 6 & 8 with 7 & 5. Knock is still on the drivers side. Really does sound like the valves, I guess I was just in denial about taking the valve cover back off.
The injector tips had an awful lot of soot on them for being run for about 30 minutes since I put them back in. Also, I'm getting a pulsing or pumping type sound at the air filter, i tired to capture it in my second video. Could those be a sign of the valve lash being off?
Definetly. On mine I had to take the passenger head back off because I had a valve not seating but mine was a LOUD thump. I still have that pumping noise you are describing though. You should roll the pushrods on a flat surface and make sure they are straight if you pull it back apart.
Ya that's the plan. Had a couple hours to do it yesterday, flew through getting it apart then stripped the valve cover bolt on the drivers side up against the firewall. Ended up getting it off by beating on it from the fender well with a pry bar and hammer, but that killed the rest of the daylight.
I should have some time tomorrow afternoon to get the valve cover off and re do the valve lash.
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Sorry it took me so long to update this. Haven't had much time to mess with the truck lately. But, finally figured it out last night. All it was was a loose injector #7. Sound has gone away and everything is normal now.
Thats what was just updated on a thread on duramaxforum, he had the same problem and found the same issue.Hopefully thats whats wrong with mine too!
Mine was the #6 intake rocker. Got it back together yesterday.