Hey guys, sorry for the delay, but wanted to follow up. Truck was at the diesel shop for 3 weeks. They ran every test possible and all completely checked out.
They were checking wiring and noticed I hooked up a Glow Shift Gauge to the Lift Pump and it was determined where I connected the gauge and sensor wiring was drawing power away from the trucks 5 volt system and the Fuel Rail Pressure Sensor took the hit.
I removed the gauge and all wiring, truck runs flawless.
At the end of the day, I want to say thank you all for your help, guidance, support and patience on this matter. I hope this forum helps someone out.