that could very well be possible because we are using the original LLY pump (that had the metal run through it from the lunched bearing).
Its a kind of a bastard trans.
02 LB7 bell housing, LLY main case and tailshaft housing, LLY internal parts/drum/etc, LB7 valve body, LLY complete pump assembly/converter flow valve, main regulator, etc..
we did not take out/clean the converter flow valve or main regulator valve/shim, we basically just swapped bell housings... the converter flow valve is the stock one; back when I built it for travis's LLY, we did not use the suncoast converter flow valve.
Maybe it will unstick itself, hopefully...I wish I had the truck right in front of me because there is a bunch of things I would like to try as far as better diagnosing it...
ben