Hi everyone! I am new to this site but not new to the Duramax. I have been fixing vehicles for 11 years. Currently I am working on a customers vehicle. It is a 2009 chevy 2500 HD with the LMM. Fass 150 GPH lift pump and Transgo shift kit. The vehicle has DSP 5 EFIlive custom tuning by Idaho Rob. Max effort tune for 530 rwhp. And also a 5 inch turbo back flow pro exhaust. My customer regularly drives the snot out of this truck. Last week Tuesday during a wide open throttle acceleration the Allison suddenly lost 4th, 5th and 6th gears. There was a P0776 Pressure solenoid 2 stuck off. A line pressure test quickly showed a massive leak as soon as the C2 clutch was commanded on. I tore the trany down yesterday fully expecting a c2 clutch seal to be torn. To my surprise the C2 seals were all ok. Further inspecting found the root cause was inside the Front support housing. The stator shaft turned inside the front support and opened the C2 clutch fluid passage to the trany lube circuit. Has any one else seen this? I am confused as to what can cause this. I want to be certain that this wont happen again. I have never hear of this before. If this is a common problem what is the fix?