Update;
Truck is back at the shop getting diagnosed for range shift inhibited issues. Trans has been shifting nice through the gears, but it’s had difficulty shifting into drive.
Took the time to order a new intercooler to remedy a suspected boost leak - I was only making 35-40 psi. Currently has the original intercoooler in it and to the best of my ability I narrowed it down to a cracked intercooler during troubleshooting.
Installed a Kennedy boost/drive combo gauge.
Made some suspension and steering changes to get this truck to launch better. Lowered it down further with lowering keys, Rancho 9000XLs, Cognito adjustable straps, Dmaxstore XD tie rods, and I went back to a factory centerlink. Also removed the overloads mainly for the ride quality and ride height - not sure the effect it has with the operation of Caltracs.
Picked up a set of Moto Metal 951s with 30x14 M&H cheater slicks. Will be saving 37 lbs per corner. Hoping to be at 6600lbs race weight.