Yeah my guy is confused too since they have went over every pipe and fitting more than once and still can't find a leak. Also fuel rail is holding 28k. AFE filter was removed during runs too. My guy has a friend in Minnesota and they apparently do a decent amount of turbo swaps on LML's. Friend said they've had great results using Motorops. So we're going to take a different approach and try out Motorops tuning. We're also seeing A LOT of smoke on bottom end. Like blacking out smoke. They think we have a vane position problem in the tuning. Who knows, we may not. PPEI has been great to deal with but somethings not right and we've gotta start deleting possibilities.