Hey all, new here but long time Duramax fanatic and fiddler. I have had some issues with my LML trans and can't seem to figure out where to go next, looking for some insight and direction! Any help is appreciated as I am a technician but not an allison guru! Long story and some weird stuff, so buckle in!
Initially pulled trans to build with DHD kit Alto/Ratiotek PRX and 1057 Suncoast- trans worked/shifted great for about 6 months of pretty hard abuse and lots of tuning clearances were within alto spec, front play was good (measured before/after). Running behind a compound turbo setup with 45 overs 700hp range.
Problems started after I did two 1-5 gear pulls a few minutes apart. No abnormal shifts/noises heard throughout the pulls. Trans shifted down through the gears fine, after I slowed to make a left turn, went to pick up the throttle at about 10mph. About the time she wanted second gear it threw a p0776 and limp 3rd. Luckily only a mile from the house, went home backed into garage. Cleared codes and restarted, put it into drive and shift range inhibited blinking indicator no forward gear. OK, tried reverse and no problem there works every time. Figured I toasted her without having much shift defuel or broke something...
Dropped pan, No metal, Transynd fluid nice bright red. Tested solenoid and circuit - all good. New filter, and preventative disassembled VB for cleaning/stuck valve inspection (VB was clean no sticking valves). Replaced ALL solenoids, harness, pressure switch w/ GM / Allison parts. Filled and fired up, still has reverse only. Drive= Shift range inhibited. Out she comes.
No oil in connectors, no issues in wiring harness as I have removed all loom and inspected harness from trans plug to tcu to ecu for frays/cuts/rubs.
Upon disassembly, C1 had slight heat discolor on one backside of friction, c2 clutches were about .03 thou worn on 3 of the discs the others speced as new, C3 and C4 about the same for wear, 3 of each missing a few thou. So, went ahead and did a refresh of all seals, frictions, steels. Alto C1/C2 Excaliber C3/C4 this time. Inspected stator for twisting, holes till at 6/12. Pump looked good no gouging there, all bushings looked good, c2 hub is sleeved and not stripped. Nothing obvious in the hard parts to a (not guru). No shavings, no bushing damage found, torrington's looked great. Went ahead and reassembled unit hoping for best but still get shift inhibited in drive, but no issues for reverse. No codes thrown with this either.
OK- so here is where it gets weird, and I don't know if this is relevant but when I bought the truck the trans temp on the DIC has always displayed -40, even though my logs and OBD port read the trans temp no problem. So, knowing the a50, I bought a new TCU thinking maybe it's going south (also to also have a backup if needed). Flashed new TCU, still get shift range inhibited but reverse is functional. I have tried stock files to make sure it isn't a tuning corruption as well to no avail. Speed sensors were ohmed on disassembly and were in spec. Turbine speed is reading good no dropouts or erratic's and comes to zero when in reverse but no drawdown in drive. I can see the oncoming clutch pressure go to 232psi on the log when put in reverse, but it takes about 3 seconds to build to 232 when putting it in drive and I see no turbine speed drawdown. VSS on my logs is showing some RPMS that I don't think are normal, when shifted into gear it will sometimes read RPM (some occasions 5krpm) on VSS which I know is not correct as I have the brakes on... so I decided to unplug the VSS to see if it would let me select drive (thinking computer seeing too many RPM preventing shift to range) reading zero VSS value and still only have reverse! Also, NO dtc is set by unplugging the vss- which I think is strange. I can also unplug my trans 20-way harness, and I still do not get a CEL...
Also, Investigated the transfer case tone wheel, seems OK, has some fore/aft play on the shaft maybe 1/4" inch or so but do not know if this is in spec. Wheels turn in reverse, so I don't think t-case is exploded or stuck in neutral. Dropped the oil on it as well, no shavngs there.
What am I missing guys? Massive hydraulic leak or comms issue? Why no p0700 dtcs? Thanks for your time if you made it this far... any help is more than appreciated.
Initially pulled trans to build with DHD kit Alto/Ratiotek PRX and 1057 Suncoast- trans worked/shifted great for about 6 months of pretty hard abuse and lots of tuning clearances were within alto spec, front play was good (measured before/after). Running behind a compound turbo setup with 45 overs 700hp range.
Problems started after I did two 1-5 gear pulls a few minutes apart. No abnormal shifts/noises heard throughout the pulls. Trans shifted down through the gears fine, after I slowed to make a left turn, went to pick up the throttle at about 10mph. About the time she wanted second gear it threw a p0776 and limp 3rd. Luckily only a mile from the house, went home backed into garage. Cleared codes and restarted, put it into drive and shift range inhibited blinking indicator no forward gear. OK, tried reverse and no problem there works every time. Figured I toasted her without having much shift defuel or broke something...
Dropped pan, No metal, Transynd fluid nice bright red. Tested solenoid and circuit - all good. New filter, and preventative disassembled VB for cleaning/stuck valve inspection (VB was clean no sticking valves). Replaced ALL solenoids, harness, pressure switch w/ GM / Allison parts. Filled and fired up, still has reverse only. Drive= Shift range inhibited. Out she comes.
No oil in connectors, no issues in wiring harness as I have removed all loom and inspected harness from trans plug to tcu to ecu for frays/cuts/rubs.
Upon disassembly, C1 had slight heat discolor on one backside of friction, c2 clutches were about .03 thou worn on 3 of the discs the others speced as new, C3 and C4 about the same for wear, 3 of each missing a few thou. So, went ahead and did a refresh of all seals, frictions, steels. Alto C1/C2 Excaliber C3/C4 this time. Inspected stator for twisting, holes till at 6/12. Pump looked good no gouging there, all bushings looked good, c2 hub is sleeved and not stripped. Nothing obvious in the hard parts to a (not guru). No shavings, no bushing damage found, torrington's looked great. Went ahead and reassembled unit hoping for best but still get shift inhibited in drive, but no issues for reverse. No codes thrown with this either.
OK- so here is where it gets weird, and I don't know if this is relevant but when I bought the truck the trans temp on the DIC has always displayed -40, even though my logs and OBD port read the trans temp no problem. So, knowing the a50, I bought a new TCU thinking maybe it's going south (also to also have a backup if needed). Flashed new TCU, still get shift range inhibited but reverse is functional. I have tried stock files to make sure it isn't a tuning corruption as well to no avail. Speed sensors were ohmed on disassembly and were in spec. Turbine speed is reading good no dropouts or erratic's and comes to zero when in reverse but no drawdown in drive. I can see the oncoming clutch pressure go to 232psi on the log when put in reverse, but it takes about 3 seconds to build to 232 when putting it in drive and I see no turbine speed drawdown. VSS on my logs is showing some RPMS that I don't think are normal, when shifted into gear it will sometimes read RPM (some occasions 5krpm) on VSS which I know is not correct as I have the brakes on... so I decided to unplug the VSS to see if it would let me select drive (thinking computer seeing too many RPM preventing shift to range) reading zero VSS value and still only have reverse! Also, NO dtc is set by unplugging the vss- which I think is strange. I can also unplug my trans 20-way harness, and I still do not get a CEL...
Also, Investigated the transfer case tone wheel, seems OK, has some fore/aft play on the shaft maybe 1/4" inch or so but do not know if this is in spec. Wheels turn in reverse, so I don't think t-case is exploded or stuck in neutral. Dropped the oil on it as well, no shavngs there.
What am I missing guys? Massive hydraulic leak or comms issue? Why no p0700 dtcs? Thanks for your time if you made it this far... any help is more than appreciated.