Truck seemed like a real toilet after I had the #2 injector replaced, found that mt PPE boost valve was clogged with debris from the hose breaking down inside I guess???? My IHI was making 48.8psi soon as we found that issue it made around 30psi again but felt real sluggish, been that way for a few weeks now, I haven't really cared bcause I have the new charger and CP3 to install, I am thinking the stock charger is getting beat and its not producing the boost fast enough???? I noticed yesterday it started feeling pretty good again I logged it today and this what I got, anyone see anything out of the ordinary? Rail Pressure looks like its ok?? actual vs desired WOT is like 500 less.
I am putting the II Silver Bullet on next week but I want to make sure everything else is ok before I start chasing my tail.
I have a reman CP3 and I bought an LBZ regulator from a member here, I planned on installing it when we do the charger. Thought my current pump was getting weak but looks ok?