EFILive log from today

JustinD

Plow Truck
Nov 21, 2008
2,067
0
36
42
Tiverton Rhode Island
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Truck seemed like a real toilet after I had the #2 injector replaced, found that mt PPE boost valve was clogged with debris from the hose breaking down inside I guess???? My IHI was making 48.8psi soon as we found that issue it made around 30psi again but felt real sluggish, been that way for a few weeks now, I haven't really cared bcause I have the new charger and CP3 to install, I am thinking the stock charger is getting beat and its not producing the boost fast enough???? I noticed yesterday it started feeling pretty good again :confused::confused: I logged it today and this what I got, anyone see anything out of the ordinary? Rail Pressure looks like its ok?? actual vs desired WOT is like 500 less.

I am putting the II Silver Bullet on next week but I want to make sure everything else is ok before I start chasing my tail. :eek:

I have a reman CP3 and I bought an LBZ regulator from a member here, I planned on installing it when we do the charger. Thought my current pump was getting weak but looks ok?
 

xcablb7

New member
Feb 8, 2009
536
0
0
Fall River
from 14.30.29.007-14.30.30.163 timing falls below 25*, at the .007 it falls all the way to 21* look at your tune see what it should be and check compensators, lotaa power left on the table there, but i do "run way to much timing and blow motors" lol
 

JustinD

Plow Truck
Nov 21, 2008
2,067
0
36
42
Tiverton Rhode Island
Truck feels pretty quick again?? :confused: Had been running good but it was real sluggish, would a FPR cause it to be a turd? Only thing I've done is add 2 quarts of 2 stroke oil to my last 2 tanks of fuel.